If you register, you can do a lot more. And become an active part of our growing community. You'll have access to hidden forums, and enjoy the ability of replying and starting conversations.

Flying Scotsman

Discussion in 'Steam Traction' started by 73129, Aug 24, 2010.

  1. Richard Roper

    Richard Roper Well-Known Member

    Joined:
    May 22, 2006
    Messages:
    1,310
    Likes Received:
    1,359
    Gender:
    Male
    Occupation:
    Librarian
    Location:
    Just up the road from 56E Sowerby Bridge
    Heritage Railway Volunteer:
    No I do not currently volunteer
    That'll be Lincoln Green then!:)

    Richard.
     
  2. class8mikado

    class8mikado Part of the furniture

    Joined:
    Jun 1, 2009
    Messages:
    3,840
    Likes Received:
    1,644
    Occupation:
    Print Estimator/ Repository of Useless Informatio.
    Location:
    Bingley W.Yorks.
    Heritage Railway Volunteer:
    No I do not currently volunteer
    Tender now de/re -wheeled, ( Pics on the works forum)
    really is a thorough going over (or did they never quite get round to checking the tender out the first time round ?
     
  3. 242A1

    242A1 Well-Known Member

    Joined:
    Dec 3, 2006
    Messages:
    1,561
    Likes Received:
    1,304
    The bigger question is whether the money and time equation ever gave anyone the chance to check everything on this engine? At least it does have a tender to call its own. Some engines are less fortunate.
     
  4. 26D_M

    26D_M Part of the furniture

    Joined:
    Oct 22, 2009
    Messages:
    4,416
    Likes Received:
    1,681
    Time is one thing this project has not been short of. Money either for that matter.
     
  5. Miff

    Miff Part of the furniture Friend

    Joined:
    Jun 17, 2008
    Messages:
    3,000
    Likes Received:
    3,023
    That question is answered by the 2012 Meanley report about the history of the overhaul up to that time, written for SMG/NRM after it became clear everything was going wrong.
    http://www.sciencemuseum.org.uk/abo...~/media/33CDC07ED88345BEA5412F91D8742D45.ashx

    And the subsequent First Class Partnerships report, which is a more detailed engineering asessment of how to go forward from that point.
    http://www.nrm.org.uk/~/media/Files/NRM/PDF/NRM Flying Scotsman Final Report.pdf

    At that time some, on this forum and elsewhere, criticised spending money on these consultants and predicted SMG/NRM would use their conclusions as an excuse to pull the plug on the funding and 'stuff & mount' the loco. Since then the work seems to have been managed much better and SMG/NRM have continued to fund the project. So I suggest bringing in the consultants at that time helped to save the project and was a very good move by the NRM.
     
  6. class8mikado

    class8mikado Part of the furniture

    Joined:
    Jun 1, 2009
    Messages:
    3,840
    Likes Received:
    1,644
    Occupation:
    Print Estimator/ Repository of Useless Informatio.
    Location:
    Bingley W.Yorks.
    Heritage Railway Volunteer:
    No I do not currently volunteer
    two tenders in fact though one has now gone onto pastures new along with a boiler. I don't remember its condition being touched on in the report(tempted to have another read...)
    I am really looking for the day she turns wheels on the mainline again, hopefully there will still be a few working drivers about from the last time around who can appreciate all the work, she must have been a bit rough and ready to handle before....
     
  7. guycarr360

    guycarr360 Part of the furniture

    Joined:
    Oct 4, 2005
    Messages:
    4,834
    Likes Received:
    3,158
    Gender:
    Male
    Location:
    Chester le Street County Durham
    Personally, think nothing is being left to chance, and with the loco's high profile, it should that way.

    Without doubt a top class job is being done, with an eye on the reliability enjoyed by the Ian Riley fleet, as a pre-requisite.

    If that is the benchmark being aimed at, we should all be happy come the end of the elongated overhaul.

    Cannot be long now.....
     
  8. 242A1

    242A1 Well-Known Member

    Joined:
    Dec 3, 2006
    Messages:
    1,561
    Likes Received:
    1,304
    There must have been little doubt that once IR and his team were given responsibility for completing the overhaul, particularly with responsibilities for the first two years of operation after the completion, that whatever could be found that required attention would receive the fullest rectification.
    The current overhaul did not commence too well but should be heading towards a fine conclusion. I am more concerned with previous overhaul work. But that is water under the bridge now. The lessons to be taken away from the current saga should prove of benefit in the years to come.
    If only the money and time had been available to allow for the frames to be fully tested and improved to allow for the impact of the improvements made to boiler, exhaust, cylinders and main steam pipes. A far from ideal application of locomotive development options but it is hard to argue with the level of power output improvement achieved. What that application did to the chassis of the locomotive is, sadly, another matter. Avoidable? Yes.
    The pressure to meet deadlines, to get the locomotive back into service cannot have been helpful.
     
  9. Big Al

    Big Al Nat Pres stalwart Staff Member Moderator

    Joined:
    May 30, 2009
    Messages:
    22,590
    Likes Received:
    22,719
    Location:
    1016
    Heritage Railway Volunteer:
    No I do not currently volunteer
    A useful 'hindsight summary' in my view. What may have changed over time is an increasing understanding of the wider engineering implications of design modifications and also the use of new solutions with old technology. Taking the long view, I don't think there is much doubt that the Scotsman saga has been a very expensive case study in that respect but at least it is something from which the whole heritage movement can learn and should learn.

    So a little more time to get it right seems a modest price to pay, I think. Looking forward to the end point.
     
  10. 26D_M

    26D_M Part of the furniture

    Joined:
    Oct 22, 2009
    Messages:
    4,416
    Likes Received:
    1,681
    The protracted nature of the overhaul means that it commenced pre austerity and the dramatic reduction in public spending. Had the commitment to commence it been at a later date its doubtful whether the amounts involved could have been sanctioned. Given an ROI expectation in the public sector of £10 per pound spent there will be an awful lot of payback expected in one form or another.
     
  11. MellishR

    MellishR Resident of Nat Pres Friend

    Joined:
    Apr 16, 2009
    Messages:
    8,912
    Likes Received:
    5,848
    The RAIB report on Tangmere's crosshead failure highlighted the replacement of a small component by a somewhat different one without adequate assessment of its suitability. Considering just how many serious faults were eventually found on FS in both the frames and the boiler, we should be grateful that none of the failures during the last few months when FS was working trains was disastrous.
     
  12. 242A1

    242A1 Well-Known Member

    Joined:
    Dec 3, 2006
    Messages:
    1,561
    Likes Received:
    1,304
    Some who have followed the fortunes of the engine over many years have been aware of the roller coaster state of the locomotive's condition. If more time and foresight had been made use of over the course of many of the previous adventures and events of earlier preservation years then this saga may not have played out in the way it has.

    If Dr. Marchington desired that the locomotive should be modified in order to achieve a higher level of performance, at one level he was right since working on the mainline raises issues. He was paying the bills, he did own the engine, but the sole survivor of an important class is not the best subject for receiving performance modifications.

    Given the history of medium/heavy modifications it is peculiar that the frames did not receive attention to make them fit to withstand the rigours of dealing with the impact of the steam circuit improvement.

    In truth if a Super "Super Pacific" was what was wanted then a new build would have been the right way to go.

    Just a few weeks to wait now. The cost will largely become forgotten. The lessons of the experience hopefully not.
     
  13. martin1656

    martin1656 Nat Pres stalwart Friend

    Joined:
    Dec 8, 2014
    Messages:
    19,263
    Likes Received:
    12,515
    Gender:
    Male
    Location:
    St Leonards
    Heritage Railway Volunteer:
    No I do not currently volunteer
    First question ,in A3 form would 4472 have been powerful enough to meet the needs of the VSOE operation? the modifications were done because this was in my view seen as some as a money cow, ie guarenteed earnings, to earn them money, and to put a little of that back into the loco, but it didnt work out that way, the engineer in charge, i dont think gave thought to the added stresses and strains that running in super power mode would bring, or mistakenly thought that it wouldnt be an issue, you must remember that at the time, this gentleman was held in high regard, so anyone asking would have thought he must know what he is doing, hindsight would indicate he may have been out of his depth .
    when 60103 steams again, hopefully in the not to distant future, all this will be largely forgotten, but the lessons must not, sensible loads behind the drawbar, a proper maintenance regime, unnder IR, i'm sure this will be the case, now after doing one LNER engine, can he be persuaded to do a second, something more simple like an Atlantic?
     
  14. Big Al

    Big Al Nat Pres stalwart Staff Member Moderator

    Joined:
    May 30, 2009
    Messages:
    22,590
    Likes Received:
    22,719
    Location:
    1016
    Heritage Railway Volunteer:
    No I do not currently volunteer
    Just so. There are many old cars sitting in scrap yards that are the living (sic) proof of what can happen when you re-bore an old engine for a bit of extra power!

    Despite the arguments on here back up-thread I can't think of anyone without the heart to wish Ian Riley and the team all the very best in doing what they do best over the next few months.
     
  15. S.A.C. Martin

    S.A.C. Martin Part of the furniture

    Joined:
    Aug 31, 2010
    Messages:
    5,615
    Likes Received:
    9,418
    Gender:
    Male
    Occupation:
    Asset Engineer (Signalling), MNLPS Treasurer
    Location:
    London
    Heritage Railway Volunteer:
    Yes I am an active volunteer
    The bizarre thing is that in LNER and BR days the A1s/A10s and later A3s all suffered with cracked frames - some worse than others - and this was regarded as a fact of life.

    Frames were replaced, sometimes 3/4 of them renewed, during the course of an overhaul and in considering the nature of Doncaster Works setup we should also remember that it was not until Cook took charge after the LNER has ceased to be that the frames of the big LNER Pacifics were set up with much better alignment and better tolerances in all of the associated components bolted onto them.

    The A3s fitted with A4 boilers have been recorded as suffering some problems in the frames, due no doubt in part to the fact the A4 boiler was heavier than the A3 type. Why this wasn't taken into account when Scotsman was rebuilt with the A4 boiler the first time around is a significant question. Bear in mind the A4 boiler was actually originally fitted around the late 80s and that the engine has spent the last twenty five years or so with the double kylchap and you're looking at a locomotive which was effectively as per many of the class in the latter days of BR steam.

    The thing that probably exacerbated the problems was boring out the cylinders and increasing the pressure of the boiler at the Marchington overhaul. Different sources cite Marchington or Kennington as the guilty party for wanting to "improve" Scotsman. I don't care to comment other than I think history should have shown those modifications without beefed up main frame strays as per the A4s was asking for trouble. We can debate this ad infinitum - and have done so - with hindsight, the fact remains that she looks to have been totally renewed this time around and that will be good for her, preservation and the NRM in that order.

    I've seen some pics on the NRM site today and I cannot wait to see her in steam, personally.
     
    Matt37401 and andalfi1 like this.
  16. class8mikado

    class8mikado Part of the furniture

    Joined:
    Jun 1, 2009
    Messages:
    3,840
    Likes Received:
    1,644
    Occupation:
    Print Estimator/ Repository of Useless Informatio.
    Location:
    Bingley W.Yorks.
    Heritage Railway Volunteer:
    No I do not currently volunteer
    Together with any ancillary waifs subjected to forces beyond the initial design....
     
  17. Jimc

    Jimc Part of the furniture

    Joined:
    Sep 8, 2005
    Messages:
    4,117
    Likes Received:
    4,821
    Occupation:
    Once computers, now part time writer I suppose.
    Location:
    SE England
    Heritage Railway Volunteer:
    No I do not currently volunteer
    I've probably asked this before, although I don't recall the answer, but were the cylinders bored out beyond what was normal on the A3s?
    Wasn't it conventional to bore cylinders larger until they reached scrapping thickness just as it is with motor vehicles?
    I recall back in my motorcycle trade days the standard manufacturer's oversize pistons took the capacity of a nominal 49cc moped up to something over 53cc, which technically made it not a moped! That was never regarded as being a big bore kit - such things would have been more like 65cc, and never especially effective unless more radical surgery was undertaken to improve the gas flow.
     
  18. damianrhysmoore

    damianrhysmoore Part of the furniture

    Joined:
    May 31, 2008
    Messages:
    2,615
    Likes Received:
    3,002
    Occupation:
    Osteopath
    Location:
    London SW8
    Heritage Railway Volunteer:
    No I do not currently volunteer
    He's done the B12/3 and the Y14 (previously J15)
     
  19. RalphW

    RalphW Nat Pres stalwart Staff Member Administrator Friend

    Joined:
    Sep 11, 2005
    Messages:
    36,447
    Likes Received:
    9,907
    Gender:
    Male
    Occupation:
    Retired-ish, Part time rail tour steward.
    Location:
    Northwich
    Heritage Railway Volunteer:
    No I do not currently volunteer
    Jimc one engine that was enlarged was the V8 that Rover got from, was it Buick? That was enlarged several times and was a very potent and for its time, reliable motor.
     
  20. Martin Perry

    Martin Perry Nat Pres stalwart Staff Member Moderator Friend

    Joined:
    Apr 15, 2006
    Messages:
    16,551
    Likes Received:
    7,897
    Location:
    1012 / 60158
    Heritage Railway Volunteer:
    Yes I am an active volunteer
    It was a Buick engine - they sold the design as it was too small for the US Market! But most US engines of that era were massively over-engineered and under-tuned for their capacity so there was much potential for improvements.
     

Share This Page