If you register, you can do a lot more. And become an active part of our growing community. You'll have access to hidden forums, and enjoy the ability of replying and starting conversations.

WW2 locomotive building.

本贴由 Eightpot2017-05-26 发布. 版块名称: Steam Traction

  1. Matt37401

    Matt37401 Nat Pres stalwart

    注册日期:
    2014-06-08
    帖子:
    15,567
    支持:
    11,981
    所在地:
    Wnxx
    Heritage Railway Volunteer:
    No I do not currently volunteer
    I'm sure commuters would have 'their' compartments too!
     
  2. Steve

    Steve Resident of Nat Pres Friend

    注册日期:
    2006-10-07
    帖子:
    12,856
    支持:
    12,097
    职业:
    Gentleman of leisure, nowadays
    所在地:
    Near Leeds
    Heritage Railway Volunteer:
    Yes I am an active volunteer
    You've only to watch old film of commuter trains arriving at the likes of Waterloo and Liverpool St to realise that the train was generally empty before it had stopped
    For example:
     
    已获得paulhitchCopper-capped的支持.
  3. Eightpot

    Eightpot Resident of Nat Pres Friend

    注册日期:
    2006-08-10
    帖子:
    8,340
    支持:
    2,506
    性别:
    职业:
    Engineer Emeritus
    所在地:
    Aylesbury
    Heritage Railway Volunteer:
    Yes I am an active volunteer
    Just very glad that I haven't had to do commuting!
     
    已获得Copper-capped的支持.
  4. paulhitch

    paulhitch Guest

    Oddly enough today I witnessed a passenger holding an outward opening door open as a train arrived at a station whilst looking at the opposite direction to the one the train was travelling. The Foreman Porter, quite rightly, was not amused!

    PH
     
  5. pete2hogs

    pete2hogs Member

    注册日期:
    2007-10-16
    帖子:
    721
    支持:
    418
    No power reverser. The GSWR men had got used to it. And also poor ergonomics - you couldn't reach the brake while looking out of the window to see the shunter, or something like that.
     
  6. pete2hogs

    pete2hogs Member

    注册日期:
    2007-10-16
    帖子:
    721
    支持:
    418
    'thought to be' is right. It's no more than a armchair theory. If that was the case you'd expect to find the tender brake hard on, for example. And some sign from the crew when they tried to apply the brakes and didn't have any - which would have been well before they passed through Grantham station. At least one witness thought steam was actually shut off and the brakes applied as they went through the station - that fits in with them not realising where they were / falling asleep and being alerted by the station itself.

    It would be a better theory for Salisbury - it would explain why the driver kept the whistle open as he approached the station - he was trying to tell people he couldn't slow down on the falling gradient with no brakes.
     
  7. Jamessquared

    Jamessquared Nat Pres stalwart

    注册日期:
    2008-03-08
    帖子:
    28,158
    支持:
    66,080
    所在地:
    LBSC 215
    Heritage Railway Volunteer:
    Yes I am an active volunteer
    One accident I can think of that was directly caused by incorrect coupling procedures when a locomotive was attached to a train was Littlehampton, 1920, in which mistakes were made connecting the air brake pipes inadvertently to the air pipes that controlled the push-pull apparatus. However, haste was not at the root of that accident, but rather because the procedure was carried out by an inexperienced man, and then not checked by anyone else. The train stood for 20 minutes after coupling before departing, during which time there was ample opportunity to correct the mistake had anyone looked closely.

    http://www.railwaysarchive.co.uk/documents/MoT_Littlehampton1920.pdf

    Tom
     
  8. paulhitch

    paulhitch Guest

    A bit more than an "armchair theory" I think but no-one will ever know for certain. It would be in the interest of a number of people for the cause to remain a "mystery".

    PH
     
  9. Jimc

    Jimc Part of the furniture

    注册日期:
    2005-09-08
    帖子:
    4,119
    支持:
    4,822
    职业:
    Once computers, now part time writer I suppose.
    所在地:
    SE England
    Heritage Railway Volunteer:
    No I do not currently volunteer
    I'm intrigued! In whose interests would it be that the cause of a railway accident 110 years ago remains a mystery?
     
    已获得Copper-cappedJamessquared的支持.
  10. paulhitch

    paulhitch Guest

    The railway company at the time it happened of course. Also the individuals whose actions/inactions were the direct cause if the theory is correct.

    PH
     
  11. Martin Perry

    Martin Perry Nat Pres stalwart Staff Member Moderator Friend

    注册日期:
    2006-04-15
    帖子:
    16,553
    支持:
    7,905
    所在地:
    1012 / 60158
    Heritage Railway Volunteer:
    Yes I am an active volunteer
    The point was why should it remain a mystery? - The company and individuals have long since ceased to be interested.
     
  12. paulhitch

    paulhitch Guest

    Oddly enough, fairly recently I did see a guard about to despatch a train without doing a brake test when he remembered his omission just in time. There had been some out of course problems that morning which is just the sort of situation when errors get made. Happily the vacuum had been properly connected!

    PH
     
  13. LesterBrown

    LesterBrown Member

    注册日期:
    2009-01-20
    帖子:
    995
    支持:
    761
    所在地:
    Devon
    How long before I get a cold call recorded message "Good morning, I understand you had a great great uncle who was killed in an accident at Grantham in 1906. Are you aware that you might be entitled to compensation.... "
     
    已获得Romsey, pete2hogs, johnofwessex另外4人的支持.
  14. sir gilbert claughton

    sir gilbert claughton Well-Known Member

    注册日期:
    2017-01-17
    帖子:
    1,062
    支持:
    511
    性别:
    职业:
    retired
    所在地:
    east sussex
    Heritage Railway Volunteer:
    No I do not currently volunteer

    yep =used to see it running light on the up local - never saw it going the other way which with hindsight was a bit odd . perhaps it was off to Camden to find a biggun
     

分享此页面