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Locomotive Management including Cylinder Cocks

Discussion in 'Steam Traction' started by MellishR, Jan 1, 2015.

  1. Sir Nigel Gresley

    Sir Nigel Gresley Member

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    The DB 044's (3-cyl 2-10-0) of Bw Ottbergen used to sit at the head of their 1500 tonne freights, especially at night, with the cocks open for about 10 minutes before departure, in order to warm the cylinders. This ensured a faultless trip over the Eggegebirge to Altenbeken, and onwards down to Hamm, but was useless for night-photography! (T-i-c)

    On the subject of slipping, northbound departures on the curve from Platform 9N at York were always interesting, as the rails were usually wet from the water column mounted in the station roof.
     
  2. chessie1

    chessie1 New Member

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    To say that the driver of BP 'did nothing to shut the regulator' is a tad unfair. As I understand it the thing had carried a lot of water over during the initial violent slip, this makes it virtually impossible to close the regulator until the water has dispersed. Also, again as I understand it, the driver had broken his wrist or arm during his initial attempt to stop the reverser going into full gear, so all in all it was a bit of a struggle on the footplate.

    As far as 4464 goes, I was on the support crew for that run...nothing untoward was reported about the start from Peterborough so unfortunately for the conspiracy theorists - nothing to see here.

    Probably just finishing his tea.....
     
  3. Steve

    Steve Resident of Nat Pres Friend

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    Saying that the driver did nothing to shut the regulator is fact. The reasons why he did nothing are a different matter. It is also fact that the driver had been reminded on several occasions previously by the NELPG rep to put the catch in. British Rail accepted the responsibility for the incident and they simply provided the crew, nothing else. The unfortunate thing is that the f/side regulator handle had been removed as a supposed safety measure. If it had been there, others might have been able to do something. I say might and not could.
     
  4. chessie1

    chessie1 New Member

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    Perhaps it would have been better if you had said that 'because of incapacity the driver did nothing etc.' I think he did his best given the lack of training and familiarity with the thing and it would appear steam locos in general.
     
  5. Big Al

    Big Al Nat Pres stalwart Staff Member Moderator

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    I've always viewed the cylinder cocks as an essential loco management and safety device. Water in the cylinders is a bad thing and anything that helps ensure it is not there must be good. I have in mind a video of a particularly fiery assault of Sapperton when what must have been some priming was picked up quickly and the cocks opened for just a few seconds to clean out. But there are times when even they can't solve the problem.

    I recall an early morning run into London on a stopper from Basingstoke with 34076 - 41 Squadron. We came to an unexpected halt and the crew then spent no less than six minutes wrestling with the steam reverser to get some forward traction. This was accompanied by clouds of steam from the cocks that completely obscured the locomotive and our destination. Yes, this all took place on a weekday morning at 8 am right across the entrance to Waterloo and opposite the signal box. Eventually, we crept rather sheepishly down to the buffer stops.

    I didn't have the heart to talk to the crew!
     
  6. Southernman99

    Southernman99 Member Friend

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    This is a perfect case of needing to open the taps. Serious priming so the driver opens up even more. There is hardly a recognisable beat towards the end of the video.

    This is mismanagement.
     
  7. marshall5

    marshall5 Part of the furniture

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    Someone who is seemingly oblivious to a loco starting to prime and doing nothing about it shouldn't be let out with a pram let alone a steam engine. There is only one way of dealing with the situation and that is to partially shut the regulator and open the drain cocks. When she has 'settled' down you can gradually open up again. If some of these so called 'drivers' had to fix (at their expense) the damage caused, or if it was their own engine, they might be more careful. It does call into question the whole business of training and 'passing out' and I am sure that it is not just at the NNR where such things happen. Ray.
     
  8. Hurricane

    Hurricane Member

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    Who removed the fireman's side regulator? Was this something BR at the time insisted on or was it much earlier on?
     
  9. Big Al

    Big Al Nat Pres stalwart Staff Member Moderator

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    Yes, contrast the above clip with this one when precautionary action is taken at around 3.15. I guess that in both cases it's a matter of listening to your loco and paying attention to what it might be telling you.

     
  10. 5944

    5944 Resident of Nat Pres

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    60009 has had her fireman's side handle removed too, but AFAIK none of the other A4s have. I believe it was removed after nearly clouting John Cameron in the head!
     
  11. guycarr360

    guycarr360 Part of the furniture

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    In late 1994, we did a footplate day at Tyseley with 4472, and Roland Kennington took over from Bob Meanley part way through.

    We asked him about the incident, and he dissected what happened, and provided a great insight in the situation on the footplate, and the hopelessness of the situation.

    I have this on a video tape, but have no means of transferring it to Youtube unfortunately, it is "gold" regarding this thread.

    As Steve also mentions, the driver had been warned about his method of driving without the reverser catch engaged between Newcastle and Durham as well.
     
  12. Southernman99

    Southernman99 Member Friend

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    Al you can see the solid white plume start and then the constant roar. Once the taps have been opened you can see the exhaust change from solid to a clear space between chimney and exhaust. Professional management. Even so, it is a rather nice sound of a Merchant working hard.
     
  13. LMS2968

    LMS2968 Part of the furniture

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    Somewhat off topic, but I've never heard No 35028 working hard before. Whenever I've seen her, she simply didn't need to!

    A very nice machine!
     
  14. huochemi

    huochemi Part of the furniture

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    There's a nice recording of it at Gresford on Railways Round the Clock (after it stops blowing off).
     
  15. Steve

    Steve Resident of Nat Pres Friend

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    I understand that NELPG removed it as a perceived 'safety' issue. It was later restored.
     

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